On this date in fire history; JANUARY 27th 1967: Apollo launch - TopicsExpress



          

On this date in fire history; JANUARY 27th 1967: Apollo launch pad fire kills 3 and loss worth $413 million (2003 dollars), Cape Kennedy, he first piloted Apollo mission was scheduled for launch on 21 February 1967 at Cape Kennedy Launch Complex 34. However, the death of the prime crew in a command module fire during a practice session on 27 January 1967 put America’s lunar landing program on hold. The crew consisted of Lt. Colonel Virgil Ivan “Gus” Grissom (USAF), command pilot; Lt. Colonel Edward Higgins White, II (USAF), senior pilot; and Lt. Commander Roger Bruce Chaffee (USN), pilot. The accident occurred during the Plugs Out Integrated Test. The purpose of this test was to demonstrate all space vehicle systems and operational procedures in as near a flight configuration as practical and to verifY systems capability in a simulated launch. It was most likely that the fire began in the lower forward portion of the left equipment bay, to the left of the command pilot, and considerably below the level of his couch. Although the Board was not able to determine conclusively the specific initiator of the Apollo 204 fire, it identified the conditions that led to the disaster. These conditions were: 1. A sealed cabin, pressurized with an oxygen atmosphere. 2. An extensive distribution of combustible materials in the cabin. 3. Vulnerable wiring carrying spacecraft power. 4. Vulnerable plumbing carrying a combustible and corrosive coolant. 5. Inadequate provisions for the crew to escape. 6. Inadequate provisions for rescue or medical assistance. As a result of the investigation, major modifications in design, materials, and procedures were implemented. The two-piece hatch was replaced by a single quick-operating, outward opening crew hatch made of aluminum and fiberglass. The new hatch could be opened from inside in seven seconds and by a pad safety crew in 10 seconds. Ease of opening was enhanced by a gas-powered counterbalance mechanism. The second major modification was the change in the launch pad spacecraft cabin atmosphere for pre-launch testing ·from 100 percent oxygen to a mixture of 60 percent oxygen and 40 percent nitrogen to reduce support of any combustion. The crew suit loops still carried 100 percent oxygen. After launch, the 60/40 mix was gradually replaced with pure oxygen until cabin atmosphere reached 100 percent oxygen at 5 pounds per square inch. This “enriched air” mix was selected after extensive flammability tests in various percentages of oxygen at varying pressures.
Posted on: Tue, 27 Jan 2015 11:57:41 +0000

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